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April
2007
At
the end of March, we had the engine long block fully assembled.
All that needed to be done was to drop the old 1300 engine
out of the Bug, swap of some bits and pieces, stick it back
in the car and bolt on some twin carbs. All sounds dead
easy doesn't it!?
Well, we had about a week to sort it out... but only a couple
of days in that could be actually spent on the bug due to
me been in West Yorkshire, and the bug been in
South Yorkshire! We had to have this done by the easter
bank holiday weekend, or I wasn't going to get to race.
The old engine was swiftly dropped out, and all the ancileries
were unbolted and cleaned up. What could be fastened onto
the new engine was fastened on. But then, nightmare. The
tin wear on the old engine, behind the pulley wheel was
different to that on the new engine. There was no hole for
the oil breather to fit through. I remembered that I had
a different oil filler neck at home, so that job was left
until last so the part could be collected and fit another
day.
Time moved on so quickly. Why is it that when you've got
a deadline, time doesn't hang around, but as soon as your
waiting for something, the seconds seem like hours. Typical!
Anyway, at the end of the 1st afternoon/evening of refitting,
the engine was pretty much built up with all its clean tin
wear on, fuel pump on, clutch on, dizzy in and timing statically
timed. It just needed the fan housing, the alternator stand
and alternator fastening on once the correct filler neck
could be sourced.
Day two of refitting saw the engine being completely built
bar the carbs. This was then slotted back into the bug...
I make it sound so simple... well the truth of it was, it
was simple. By far the easiest engine refit I've done to
date. I found the trick lies in getting the car body level,
that way your not fighting with the engine on an angle to
get the clutch to slip onto the gearbox input shaft.
once the engine was in place, the fixing in position of
the carbs could commence. The carbs had previously been
on a 1600 that I took off the road a few years back due
to the dreaded tin worm, but alas, they had found a new
ride to sit on. I thought that due to the carbs previously
been professionally set up on a rolling road on my 1600,
I'd leave them as they work, because theoretically, they
should be ready for this new engine.
Refitting of the carbs, as always with the fiddly little
spaces to get your hands in, was a right royal pain in the
rear. A couple of hours later, and an aching back to prove
it, the engine was in, and built. Completed. Yay! Time was
getting on now though, and the neighbours didn't look too
pleased when I walked down the drive with ear defenders
in hand ready to fire the new engine over. We made a decision
to wait till the next day to do that. Safer not to upset
the neighbours ;-)
The next day came, the fuel lines were connected up, the
battery was reconnected. We turned the engine over a few
times without spark plugs in. We did this for two reasons.
Firstly, the oil needed to be pumped round the engine and
secondly, we needed to get fuel through the system and up
to the carb float chambers. Once we were happy that things
ticked over, the spark plugs were fitted, the HT leads were
connected up, and with a blip on the throttle, the engine
roared into life. I'd done it... I'd completed my first
engine build and it worked. I was so chuffed.
We warmed the engine up, and had it run for 20 mins at 2000
rpm just to help run in the new bearings and the like. Then
as we'd used a Bosch 009, the timing needed to be checked
at 3000rpm to make sure that it hit the right advance. All
was good.
-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-
Once we were happy with the engine running at idle, we took
it out for a short spin. Everything was good, apart from
the clutch. It was slipping. A quick tinker with the cable
released some tension, and the slipping stopped. We were
over the moon.
The oil was changed, and the car was taken on it's maiden
voyage, across Sheffield. It'd been so long since I had
driven a bug. It felt really weird at first, but I soon
got back into the swing of things. The bug made it, a few
miles under its belt without any hiccups. The next day was
it's first real test, we wanted it to take us to Matlock
Baths which it did. Only this time out, I noticed that the
accelerator was sticking slightly, so when we were in traffic,
the engine wanted to rev its nuts off! After a bit of investigation,
I found that the accelerator cable cover, the one that should
be held in place by two 17mm bolts, was infact held in with
1 bolt, and a blob of silicone! Agghh! After a bit of pokeing
around, and a liberal application of spray grease, things
were a little better, but the Weber 34ict throttle return
springs leave a little to be desired, so a new contraption
was put together to aid the return of the throttle... in
true Kooky style!
-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-
It was now easter weekend. The weekend of Beetles Vs Minis
at York Raceway. So, we loaded up the camper with tools,
just in case, and headed off to York. Arriving on saturday
night, we set up camp, and got in an early night ready for
my first attempt at drag racing the following morning.
Sunday morning arrived, and bright and early, I took the
beetle to scrutineering. Everything was checked over to
makes sure that we were safe to race, and then I could sign
on and be given my racing number... V29.
Results of my Sunday racing in the Beetles Vs Minis Shootout
can be found here:
http://yorkdragway.intrica.co.uk/results.pl?date=2007-04-08;car=V29
As you can see, the times were certainly not spactacular,
and were approx 2-3 seconds slower than I anticipated. Saying
that, I still manage to win my round of the shootout, scoring
a much needed point for the Beetles! Yay! After the racing
had finished, I pulled the bug up in the pits, and while
enjoying a nice cold beer, I investigated the engine to
see why times were so slow. I checked over the timing, everything
was spot on. I checked over the fueling, that seemed fine
too. The carbs were evenly tuned. I was a bit confused.
It wasn't until I ran a compression test, I found out what
was causing the slow runs. On cylinders 3 and 4, the engine
was running a very healthy 120psi, however, on 1 and 2,
it was only managing 60psi.
I checked the torques on the headbolts. Everything seemed
in order there. There were no visiable oil leaks around
the pistons of the heads that could of indicated a warped
head. The valve gaps were all spot on, so I decided that
maybe the piston rings could be aligned so that all the
gaps were in the same place, allowing the gases to flow
by.
Never the less, I was a little naughty. The engine was bolted
back together and the car was put to bed for the night ready
to try racing again on the Monday in the Air Cooled Eliminators.
For the first weekend of racing, I was really happy with
myself. I'd managed to get my reactions down to 0.7 seconds,
and seemed to be running pretty consistant times. I qualified
in 3rd, but lost in the semi-final against Darren in his
11 second bug. I've got some in car video of this run, and
it shows just how close it was as he passes me while the
finish line is so near! I'll have in next time ;-) Results
from the Air Cooled Eliminators - Round 1 can be found here:
http://yorkdragway.intrica.co.uk/results.pl?date=2007-04-09;catagory=I
Thats in for April. The bug came home, and sat under wraps
until time could be found to drop the engine and investigate
the compression problem.
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